Register now to get rid of these ads!

Projects Belly Tank Build UK

Discussion in 'Traditional Hot Rods' started by JamieUC, Jan 3, 2021.

  1. JamieUC
    Joined: Jul 8, 2013
    Posts: 175

    JamieUC
    Member
    from Swansea UK

    Apologies for the lack of updates I've been super busy with work, which is good.
    Been making some upgrades to the tank ready for Pendine, superchargers on and I had first drive around the carpark yesterday since fitting it. Also been working on the body work...
    PSX_20230528_203357.jpg

    20230527_145804.jpg

    20230527_145748.jpg
     
  2. 282doorUK
    Joined: Mar 6, 2015
    Posts: 473

    282doorUK

    It's coming along very nicely now Jamie. The cage cover looks good and I'm now wondering if a perspex bubble is in the plan, no more sand in the teeth. :D
     
    Last edited: May 28, 2023
    JamieUC likes this.
  3. The best looking new build Tank there is hands down, a total credit to you. Will be eagerly waiting for the real test on the sands of Pendine......can't wait.:cool::cool::cool::cool::cool::cool::cool::cool::D JW
     
    JamieUC likes this.
  4. See y’soon Jamie! Looking good!
     
    JamieUC and 26 T Ford RPU like this.
  5. brady1929
    Joined: Sep 30, 2006
    Posts: 9,436

    brady1929
    Member

    That is very cool.
     
    JamieUC likes this.
  6. Besty34
    Joined: Sep 9, 2010
    Posts: 429

    Besty34
    Member

    love how you have hidden the cage, some cars look ridiculous
     
    JamieUC and hotcoupe like this.
  7. Bandit Billy
    Joined: Sep 16, 2014
    Posts: 13,804

    Bandit Billy
    ALLIANCE MEMBER

    Could there be a sort of removable golf club carrier on the side? It's that close to perfect.
     
    JamieUC likes this.
  8. Dave G in Gansevoort
    Joined: Mar 28, 2019
    Posts: 3,093

    Dave G in Gansevoort
    Member
    from Upstate NY

    Beautiful lines. That rollcage fairing is perfect.
     
  9. JamieUC
    Joined: Jul 8, 2013
    Posts: 175

    JamieUC
    Member
    from Swansea UK

    Got busy punching louvers this weekend, some to add ventilation for the driver compartment, as Burnard (282dooruk) has guessed I'm planing a lexian/ perspex bubble canopy, and some around the carburettors for air intake,
    No fancy press for these just a bolt on die and handheld punch, it's very labour intensive and you have to weld up all the bolt hole that align the die but it gets the job done.
    20230603_112941.jpg

    20230603_112933.jpg

    20230603_151722.jpg
     
  10. What a cool idea!! The way i see it, if they all face back they will act as extractors and cause a low pressure on the inside, only air getting in will be from axle and exhaust cutouts, the faster you go the more effect there will be. JW
     
    Last edited: Jun 4, 2023
    JamieUC likes this.
  11. Besty34
    Joined: Sep 9, 2010
    Posts: 429

    Besty34
    Member

    love the louvers
     
    JamieUC and 41 GMC K-18 like this.
  12. brepil
    Joined: Oct 4, 2011
    Posts: 42

    brepil
    Member

    Looks superb Jamie, top job.
     
    JamieUC likes this.
  13. JamieUC
    Joined: Jul 8, 2013
    Posts: 175

    JamieUC
    Member
    from Swansea UK

    Well Pendine has been and gone and was not a great success for me and the tank, I got two runs on the Saturday, I was really excited as all seemed well the supercharger was boosting well and the engine sounded lovely.....first run and It pulled like a train in second but on the change to third I lost traction and by the time I got traction again it just seemed to bog down. The speed came through at 97mph which to be quite honest I was a little disapointed after fitting the supercharger I was expecting over the 100mp.
    So on too run number two and I was thinking give it the beans/long shift into third and hopefully power into the hundred mile an hour club..all was going well pulling like a train in second third gear change at about 75mph, at this point boost pressure was around 10psi ,and it all went wrong lost power and just about managed to get a time of 94mph.
    On the run back it was obvious something was wrong and when I stoped in the pits water was pouring out of the exhaust.
    Thinking I'd probably blown a head gasket and could possibly be in the running for Sunday me and Steve my good buddy and chief pit crew boss headed back to the workshop to get a spare head gasket and some tools. By the time we got back the belly tank had cooled down so we set about taking the head off but inspection of the head gasket revealed no faults and closer inspection of number six cylinder revealed a nice hole in the cylinder wall that I could almost get my finger in.
    So there ended the racing for the weekend, It was getting late and with no chance of racing on sunday the only thing left to do was head to the Springwell pub have several beers which turned into a cracking good night.
    The engine could be sleaved but I also have a spare block that I'm going to magnaflux and pressure test this week, before I make my mind up whether to repair the existing block or start again.

    What I've learnt form this is don't be too gready on the piston size and keep the boost a litle lower.:cool:

    Although blowing up the engine was a bit of a downer I still had a great weekend and have to say a big thanks to Neil, the Sidewinders, the people of Pendine and everybody involved in making this superb event happen.
     
  14. THE FRENCHTOWN FLYER
    Joined: Jun 6, 2007
    Posts: 5,662

    THE FRENCHTOWN FLYER
    Member
    from FRENCHTOWN

    Bummer.
    I saw you run on the Pendine thread video and saw the smoke / steam near the end.
    Good luck with a new engine combo.
     
    41 GMC K-18 and JamieUC like this.
  15. 282doorUK
    Joined: Mar 6, 2015
    Posts: 473

    282doorUK

    Proper bad luck there Jamie, but one good thing is that it didn't chuck lumps out through the tank.
     
    41 GMC K-18 and JamieUC like this.
  16. alchemy
    Joined: Sep 27, 2002
    Posts: 21,475

    alchemy
    Member

    Look at it this way: You went 97 and 94 MPH on seven cylinders!!!
     
  17. Little Terry
    Joined: Oct 17, 2007
    Posts: 699

    Little Terry
    Member

    It's a real shame that Jamie. The car looked and sounded great on the first run, but I could see it was a bit squirrelly. I missed your second run so didnt realise you had a problem. I was very surprised not to see your name on the 100mph club list!
    At least it wasn't any more catastrophic than blowing the block.
    Here's some footage....
     
  18. Besty34
    Joined: Sep 9, 2010
    Posts: 429

    Besty34
    Member

    Bad luck but you will be back, I ran ( if I remember righty ) 99.98 mph before going back the next year to run over the ton and claim my t-shirt.
     
    JamieUC likes this.
  19. Bad luck indeed, but it looked and sounded so good. As i recall, all the cylinder walls were rather thin so if you do re sleeve as i am sure the rest of the block checked out good and all the other work you did to it, i hope you do all eight and reduce the piston size. Look forward to following the rebuild. JW
     
    JamieUC likes this.
  20. JamieUC
    Joined: Jul 8, 2013
    Posts: 175

    JamieUC
    Member
    from Swansea UK

    Hi JW I think your right best way to go if I repair the block is probably to sleave all eight and not be so greedy on my piston size.

    I like your perspective.

    Thanks for the Video Marc, and as you say its only blowing a block could be a lot worse, saw a guy spin a very nice 32 roadster last weekend at the MPH sprints, bloke was OK but the roadster was definitely worse for ware.
     
  21. Mart
    Joined: Mar 3, 2001
    Posts: 4,947

    Mart
    Member

    Yes, I was sorry to hear of your misfortune. I know you will come back stronger and faster next year. having your own boring bar is certainly an advantage for you. Good luck with it.
     
    JamieUC and 26 T Ford RPU like this.
  22. JamieUC
    Joined: Jul 8, 2013
    Posts: 175

    JamieUC
    Member
    from Swansea UK

    Quick vid of my first run at Pendine this year
     
    hotcoupe, AndersF, Jeff34 and 10 others like this.
  23. Harv
    Joined: Jan 16, 2008
    Posts: 1,231

    Harv
    Member
    from Sydney

    Now that is cool

    The run-in and run-out noise reminds me of WW2 aircraft taxi-ing.

    Well done sir.

    Cheers,
    Harv
     
  24. Damn that's cool, seemed to be pulling well. Great vid. JW
     
    JamieUC likes this.
  25. JamieUC
    Joined: Jul 8, 2013
    Posts: 175

    JamieUC
    Member
    from Swansea UK

    Gearing up for this years Pendine races, I've been putting together a new engine over the winter and finaly got it ready to go in the tank. very similar specks to last one 4" merc crank, Ross 3 5/16" forged pistons, billet center main cap line bored to match, Isky Max one cam with Manley valves and springs.
    Body coming off, makes it alot easyier to work on the engine.
    Tank 177.jpg

    Tank 178.jpg
    Tank 179.jpg
     
    Chalkie, brEad, RatPwrd and 13 others like this.
  26. Love the race footage, thank you.
     
    JamieUC likes this.
  27. 282doorUK
    Joined: Mar 6, 2015
    Posts: 473

    282doorUK

    Marvellous, can't wait to hear it roar!
     
    JamieUC likes this.
  28. Look forward to round three and watching more development on the Tank. I'm about to give mine a fright and get stuck into it. JW
     
    loudbang likes this.
  29. brady1929
    Joined: Sep 30, 2006
    Posts: 9,436

    brady1929
    Member

    Your tanker is awesome. Good luck.
     
    JamieUC likes this.

Share This Page

Register now to get rid of these ads!

Archive

Copyright © 1995-2021 The Jalopy Journal: Steal our stuff, we'll kick your teeth in. Terms of Service. Privacy Policy.

Atomic Industry
Forum software by XenForo™ ©2010-2014 XenForo Ltd.