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Projects Father/Son 29 RPU - first build

Discussion in 'The Hokey Ass Message Board' started by TBone69, Jul 21, 2013.

  1. bct
    Joined: Apr 4, 2005
    Posts: 3,154

    bct
    Member

    great thread!!
     
  2. MJW
    Joined: Jun 29, 2006
    Posts: 474

    MJW
    Member
    from NJ
    1. PA. NJ. local HAMBERS group

    Interesting. I think the stock A spindles are the same as '39 and up. I used the hoop on my Lakester but had juice brakes. See you at TROG.

    Sent from my Nexus 6P using The H.A.M.B. mobile app
     
    brEad likes this.
  3. Just found your thread. Great job involving your son. I failed to plant that seed early enough with my three boys.
     
    TBone69 likes this.
  4. TBone69
    Joined: Aug 21, 2007
    Posts: 833

    TBone69
    Member
    from NJ

    Had a great Father's Day, started with a BIG breakfast, watched some hot rod shows, found The Race of Gentlemen Pismo Beach and and Midwest Fabrication on Amazon. Then braved the swamp like humidity in NJ yesterday and spent quality Father/Son time in the garage.

    First up was to tap the tie rod deeper so the tie rod ends would turn all the way in to correct the massive toe out. We did both RH and LH sides using the appropriate taps, 11/16-18 RH and LH

    upload_2017-6-19_9-19-32.jpeg

    Tie rod now turns in all the way
    upload_2017-6-19_9-22-3.jpeg

    Then it was time to figure out how to mount the hoop steering arm onto the 36 spindle. We stripped the brakes off and it was determined to leave the spindle mounted and drill out the upper two mounting holes to 1/2"

    upload_2017-6-19_9-23-55.jpeg

    Had to drill it out in sized steps and used plenty of cutting fluid and the real drill as the cordless was not up to the task. My son held the machinist square to make sure I drilled a straight hole and here is the end result.

    upload_2017-6-19_9-25-56.jpeg

    There is not much "meat" left on the corner but I think with everything bolted up we will be ok. If you have a different opinion I would like to hear what you think/know.

    The hoop steering arm was a little to wide so time to give it a squish. Mounted it in the BIG vise and gave the handle a few cranks.
    upload_2017-6-19_9-28-15.jpeg

    On the second try it fit like a glove, happy dance and much celebration not shown :)
    upload_2017-6-19_9-29-32.jpeg

    I then drilled out the grease shield and put my son to work cleaning up the holes with a file to get the pieces to fit nicely.
    upload_2017-6-19_9-30-20.jpeg

    upload_2017-6-19_9-30-44.jpeg

    Got everything bolted back up and everything clears and the chassis now goes straight with both tires pointing straight ahead! It was hot n humid and we were both overheated, cleaned up and went to the movies to see The Mummy to cool down.

    upload_2017-6-19_9-33-19.jpeg
    upload_2017-6-19_9-33-43.jpeg

    Time to order some parts and finish up the rolling chassis then onto the engine!
     
    brEad, Aaron D. and kidcampbell71 like this.
  5. Nice work. Good to see your son helping!
     
  6. TBone69
    Joined: Aug 21, 2007
    Posts: 833

    TBone69
    Member
    from NJ

    Ok it was one of those 2 step backwards and not even 1 step forward weekends.

    Ordered a bunch of parts discovered u need to change the rear mechanical brake arms from the 36 style which angle in to the model A style. Tried for about an hour to remove some model A arms I have, gonna order some new ones.

    So today I figure I would rebuild the brake cross shaft.

    Got it disassembled and clear up. Had to drill out the pins.

    [​IMG][​IMG]

    I got the repair kit with steel sleeves and new oversized busihings. One sleeve was longer than the other. Turns out one side of the cross shaft is longer too.

    Got everything text fit and sleeves loctite'd one

    [​IMG][​IMG][​IMG]

    Pin holes in the arms were egged out, welded them up and re drilled, forgot end result pics but they now fit with no slop
    [​IMG][​IMG]

    Got it all back together and just finished peeling over the last pin when I noticed I put one side on upside down. Rrrrrrtrrr
    [​IMG]

    Once temper tantrum subsided I called it a day, time to clean up and cool down with a cold one and a dip in the inlaws pool




    Sent from my iPhone using The H.A.M.B. mobile app
     
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  7. bct
    Joined: Apr 4, 2005
    Posts: 3,154

    bct
    Member

    I learn everything the hard way too.
     
  8. It used to be I only made mistakes when I was just starting a task and was eager to dive in, and also toward the end of the task when I was tired and should have stopped a half-hour earlier. Then I began to realize there wasn't a sweet spot between the two, and that I was just constantly making mistakes. Oh, well.
     
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  9. TBone69
    Joined: Aug 21, 2007
    Posts: 833

    TBone69
    Member
    from NJ

    Got a bunch more parts delivered during the week and it was hot this weekend and I was a little lazy on taking pics but progress was made.

    Saturday was one of those learning experiences.
    Started by fixing my previous mistake of putting the arm on upside down on the brake cross shaft. Once that was completed I taped it off and handed it to my "painter/helper/gopher" told him to take it easy and paint with light coats and don't soak it in paint :)

    While he was painting I go to tackling swapping that rear brake arms over to Model A style. Not sure if I explained why previously so I'll do it here. The 36 style brakes had the brake equalizer in the center of the chassis so the rear brake levers are angled in.
    upload_2017-7-10_14-49-37.png

    Had to remove the rear "Bone" to drill out the pin holding on the brake lever. After much drilling and sweating in the hot sun I was finally able to remove the stock arm.
    upload_2017-7-10_14-52-7.png

    Now on to fitting the replacement Model A style arm. Just like everything else in this project it needed some tweaking. The arm slide on but the holes for the pin did not line up. After some filing on the bottom of the arm the holes aligned, pinned and peened.
    upload_2017-7-10_14-55-41.png

    At this point I we took a lunch break and went inside to cool down and rehydrate. Once cooled and fueled we headed back out and this is where the lack of pictures, and learning experience came in. I headed over to the other side removed the other bone and said wait a minute let me check and make sure the Model A brake lever clears the rear bones. Well it didn't couldn't even make it work.

    Had to walk away for a few minutes and grab a cold one and contemplate our next step. Well I got to thinking the original brake arm is probably forged and made of good steel and I have cold bent front axles back into shape so why not this stupid little brake arm. I put it in the vise and with a Big Ass Pipe Wrench I gave it a twist and holy crap the arm was now angled straight.

    I removed the Model A Arm and resintalled the original Arm, then off to the other side left the arm attached and used the same Big Ass Pipe Wrench and gave it a twist straight. Now after using all my hulk like strength to bend metal to my will I was spent and reassembled the bones, brakes, put the wheels on rolled the chassis into the garage.
     
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  10. TBone69
    Joined: Aug 21, 2007
    Posts: 833

    TBone69
    Member
    from NJ

    Day 2 Sunday, hit the garage with a positive attitude and main goal was to install the brake rods.

    First up install the front brake cross shafts. After messing around trying to figure out how to get them installed I figured out by taking out the king pin locking bolt, rotating the king pin the shafts slipped right in. Got my main man tightening things up.

    upload_2017-7-10_15-11-23.png

    Next up install the freshly rebuilt and painted main brake cross shaft. Only took us two tries as we mounted it backwards the first time around. Told my son this is how you learn now take it off and put it back on. :)
    upload_2017-7-10_15-13-23.png
    upload_2017-7-10_15-14-4.png

    Ok now onto figuring out on how to mount the brake rods, since this is my first time installing them. I had all new parts and test fit everything together. Well the new brake clevises did not fit without a little filing. Looks like they are as cast and needed some smoothing to function properly, a little work the file and they where good to go.

    One other head scratcher during the install was one brake rod seemed too long and one to short until I realized the wishbone wasnt centered, once I straightened that out it was all good.

    Before
    upload_2017-7-10_15-17-57.png

    After - File, test fit, Repeat
    upload_2017-7-10_15-18-37.png

    Front rods mounted and working
    upload_2017-7-10_15-19-45.png
    upload_2017-7-10_15-20-17.png

    Now on to the backs. Being that the rear brakes are '36 and the arms are in a different location I knew I was in for some more work, but it wasn't bad as I thought. The rods were a couple inches too long. But with plenty of thread to play with the whizzer wheel made quick work out if.

    upload_2017-7-10_15-22-19.png
    upload_2017-7-10_15-22-48.png
    upload_2017-7-10_15-24-33.png

    Now one thing I still need to do is to move or make a new mount for the return spring/anti rattle "thingies" for the rear that pull the brakes off.

    Extremely pleased with ourselves we cleaned up and called it a day. Just waiting on rear wheel/axle bearings which hopefully should be here this week we can button up the chassis this coming weekend. Will still need to rebuild the steering column and get that mounted but we are close.

    Next major piece of the puzzle will be the Banger, my son has been dying to get started on it.
     
    loudbang, bct and brEad like this.
  11. You guys are making good progress. And spending some real quality time with your son.
     
    loudbang likes this.
  12. TBone69
    Joined: Aug 21, 2007
    Posts: 833

    TBone69
    Member
    from NJ

    Picked up a motor from a friend. It had run but had a bunch of blow so our goal was to get it mounted on a stand and pop the head.

    First up was assembling the engine stand.

    [​IMG]

    Next up was to build a bracket to mount to the stand. Got my chief mechanic removing pan bolts

    [​IMG]

    We grabbed a piece of angle iron and fashioned it into a bracket to bolt to the rope of the pan rail. Some drilling and grinding and viola.

    [​IMG]
    [​IMG]

    A trip to the parts store to grab some bolts.

    [​IMG]
    [​IMG]

    Now to make some spacers, dug into the scrap pile and found a few pieces I could use, just part them to length

    [​IMG]
    [​IMG]

    All bolted up. Now to lift onto the stand.
    [​IMG]

    Engine hoist connected and unbolting engine from its cradle.

    [​IMG]

    Engine on the stand so let's pull the head.
    [​IMG]

    Head off someone had been in here before tops of pistons had marks from a punch and tops of pistons had heavy scrape marks. Pistons very loose in the bores, looks like more than a ring job will be needed.




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  13. TBone69
    Joined: Aug 21, 2007
    Posts: 833

    TBone69
    Member
    from NJ

    Got the video of inspecting the pistons once we got the head off posted up to you tube. Side to side movement seem excessive, slight ridge on the cylinders.

    We will dig deeper this coming weekend.

     
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  14. TBone69
    Joined: Aug 21, 2007
    Posts: 833

    TBone69
    Member
    from NJ

    Took some measurements of the bores this evening, well first two any. I used some cheap harbor freight telescoping gauges and a digital Veneer caliper so it may not be super precise but the readings were repeatable.

    Pistons do have a 60 over marking on them but bores are coming out with .070 plus

    I'm going to check the bottom end this weekend in hopes the Babbitt is good and I can just get away with a reborn. If I can I'll take it to .100 over. As they say there's no replacement for displacement, hahaha


    [​IMG]


    Sent from my iPhone using The H.A.M.B. mobile app
     
    Last edited: Aug 7, 2017
  15. bct
    Joined: Apr 4, 2005
    Posts: 3,154

    bct
    Member

    Great thread , thanks for the update.
     
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  16. TBone69
    Joined: Aug 21, 2007
    Posts: 833

    TBone69
    Member
    from NJ

    Wow I haven't added updates in almost two years! Picked up a motor last August of '18 and dropped it in and got the steering mocked up.

    While perusing Instagram one morning I found a great deal on a motor about an hour away. Fellow HAMB member swapping to a flathead. Came home with Motor and a side shift 40 trans.

    She's been rebuilt .040 over, new valves and seats, adjustable lifters, aluminum cam gear and if I remember correctly an H&H cam. Motor had duals, high compression head and header on it when running.
    upload_2019-7-2_14-43-59.png

    Then I got my helper and put him to work mounting it on a stand.
    upload_2019-7-2_14-44-58.png

    First order of business was to swap over to the early front timing cover for the solid mount cross member.
    upload_2019-7-2_14-48-17.png


    Now while doing this of course I dropped sh*t down in the pan, had to pull that and everything looked great inside.
    upload_2019-7-2_14-49-47.png

    Next up, clean the deck and swap out the long head studs to the stock length to mount the head I have. Plans are for a high compression head in the future, at the time funds were limited, so stock it was.

    upload_2019-7-2_14-51-13.png

    Studs removed and deck cleaned up
    upload_2019-7-2_14-51-50.png

    Stock studs installed
    upload_2019-7-2_14-52-32.png

    Head came with plugs installed, had to use Ford spark plug wrench for authenticity

    upload_2019-7-2_14-53-32.png

    More to come.
     
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  17. TBone69
    Joined: Aug 21, 2007
    Posts: 833

    TBone69
    Member
    from NJ

    While I'm replacing gaskets why not change the valve cover gasket while we are at it. It was a HOT sunny day so we borrowed the patio furniture umbrella for some shade.
    upload_2019-7-2_14-55-54.png

    Hey look at that adjustable lifters, it's a Hot Rod Banger Baby! :)
    upload_2019-7-2_14-56-31.png

    Time for a new head gasket. New copper gasket coated in copper coat dropped on and ready for the head. Not sure what my son is doing but that's his leg on the right.

    upload_2019-7-2_14-57-44.png

    Ok time learn a lesson on how to torque the head. Yes he likes imports too.

    upload_2019-7-2_14-59-12.png

    All buttoned up, well almost
    upload_2019-7-2_15-1-6.png

    Seemed to be a leak from the rear so we removed the flywheel and flywheel housing and cleaned things up. Forgot to take the before but the gasket around the end of the cam was indeed leaking.
    upload_2019-7-2_15-4-24.png

    And found this while cleaning up the clutch housing. Crack on each side.
    upload_2019-7-2_15-5-28.png

    Luckily I had a couple more housing laying around and picked the best out of the two. Ya she has a chunk out of the bottom but this is where the weep hole is anyway it's just better flowing now :)
    upload_2019-7-2_15-6-35.png

    more in the next post
     

    Attached Files:

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  18. TBone69
    Joined: Aug 21, 2007
    Posts: 833

    TBone69
    Member
    from NJ

    Time to paint the motor. Since this project is no where near stock and a Hot Rod I found no need to go with the original Ford Green. Plus my local store didnt have any and whats better than a Red Hot Rod? A Red Hot Rod Engine and yes it is Ford red so all is good. Plus I hear painting your engine red adds 5HP :)

    Getting things taped off and prepped for paint
    upload_2019-7-2_15-10-27.png

    upload_2019-7-2_15-10-43.png

    Rattle them cans and start spraying.

    Yes I am going with the Red and Black motif and I know it's over done, but I like it and it's my build so I will paint it red and black. I say this all in jest :)

    Don't worry there will be a nice aluminum head, side cover and intake down the road to really set it off.
    upload_2019-7-2_15-11-25.png

    upload_2019-7-2_15-12-22.png

    Cant forget about the flywheel housing.
    upload_2019-7-2_15-12-50.png

    Had to start dropping some parts on it to get the juices flowing, paint job came out pretty good, I think.

    upload_2019-7-2_15-16-38.png

    Next post mounting and shimming the flywheel housing.
     
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  19. TBone69
    Joined: Aug 21, 2007
    Posts: 833

    TBone69
    Member
    from NJ

    Ok so the flywheel housing I pulled off was cracked so I am thinking it wasn't shimmed correctly flexed and cracked when tightened down.

    First steps clean up the mating surfaces.
    upload_2019-7-2_15-19-6.png
    upload_2019-7-2_15-19-27.png

    Bolt up housing to back of motor. Notice the gap between the motor block and upper bolt holes.
    upload_2019-7-2_15-20-3.png

    Picked up a digital dial indicator and took some initial measurements before tightening the upper mounts.
    upload_2019-7-2_15-29-9.png

    Now tighten upper mounts and take another reading.
    upload_2019-7-2_15-21-52.png

    I had previously ordered 4 .010 shims thinking 2 each side should be good but I was off .016. So I did what any shade tree mechanic would do, I made my own out of some roofing flashing.

    upload_2019-7-2_15-31-1.png

    With the shims, cut down piece of flashing and throttle assembly bolted down and tightened we came in on the money!
    upload_2019-7-2_15-32-16.png

    Next up lets drop this puppy between the frame rails!
     

    Attached Files:

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  20. TBone69
    Joined: Aug 21, 2007
    Posts: 833

    TBone69
    Member
    from NJ

    Sept 15th 2018 the motor is going in!

    Engine hoist assembled and getting ready to take engine off the stand. You can see my home made shim, maybe I'll replace it with smaller shims, maybe I'll paint it or maybe I won't do anything to it.
    upload_2019-7-2_15-34-31.png

    My helper forgot to tighten the bolts on the hoist

    upload_2019-7-2_15-36-9.png

    Up Up and Away
    upload_2019-7-2_15-36-43.png

    Set it back down on the floor so we can remove the home made mounting brackets for the engine stand.
    upload_2019-7-2_15-37-36.png

    At this point my main mechanic is steering the hoist and I'm guiding the engine home so no pics of the actual act, maybe my Wife has video, I'll see if I can find it.

    Motor is in the frame! My chief mechanic is hard at work bolting the mounts together.
    upload_2019-7-2_15-40-41.png

    upload_2019-7-2_15-41-20.png

    Car's not quite ready for TROG but this guy is!
    upload_2019-7-2_15-42-20.png

    And that's where we finished up the 2018 season.
     
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  21. TBone69
    Joined: Aug 21, 2007
    Posts: 833

    TBone69
    Member
    from NJ

    Wow July 2nd and getting ready for a nice long 4th of July weekend!

    Not much work so far but picked up a lightened flywheel setup for 9" V8 clutch and a 37 top loader trans that will get cleaned up and mounted via a clings adapter.

    Then BIG purchases planned for 2019 stay tuned.
     
  22. TBone69
    Joined: Aug 21, 2007
    Posts: 833

    TBone69
    Member
    from NJ

    Quick update

    Picked up 37 trans to run behind the Banger.

    I’ll start a full rebuild thread at some point

    Started with this

    [​IMG]

    Lightened , balances flywheel, V8 clutch and a Clings adapter.

    [​IMG]

    Bunch of cleaning and parts later and hope to have the trans back together tomorrow .

    [​IMG]

    Had to mock it up in the chassis

    [​IMG]







    Sent from my iPhone using The H.A.M.B. mobile app
     
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  23. Atwater Mike
    Joined: May 31, 2002
    Posts: 11,624

    Atwater Mike
    Member

    Love this project! My #1 son, Rich and #4 son, Tory are into early hot rods, we all have '55 F100s, for dragging home 'stuff'...
    Great project here, proud of your son, and the experience he is devouring!
     
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  24. bct
    Joined: Apr 4, 2005
    Posts: 3,154

    bct
    Member

    i too admire your family project.
     
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  25. TBone69
    Joined: Aug 21, 2007
    Posts: 833

    TBone69
    Member
    from NJ

    Picked up a "Hot Rod" gas tank. I was out antiquing with my wife this weekend and scored this O2 tank for $40!

    It was being sold as a bouy and by the looks of it was being used as one.

    IMG_5376.JPG

    Still a few specks of the original yellow/mustard paint

    IMG_5378.JPG


    Sent from my iPhone using The H.A.M.B. mobile app
     
  26. TBone69
    Joined: Aug 21, 2007
    Posts: 833

    TBone69
    Member
    from NJ

    Transmission has been kicking my butt for the past two weeks it would rotate then lockup. Couldn’t figure it out the. Had an ah ha moment yesterday.

    Transmission was acting like it was in two gears at once, as soon as I moved the sliding gear in neutral I could turn the input shaft.

    I had two issues. The first being the early style synchro has a sweet spot where it just slides on the main shaft and one were it needs persuading. Must be on the sweet spot so it slides on the shaft. Issue two was the way I had the trans mounted in the vise at and able. The synchro hub would slide back and grab 2nd gear as I was testing reverse or first.

    Now on to rebuild the shift tower!

    IMG_5425.JPG


    Sent from my iPhone using The H.A.M.B. mobile app
     
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  27. bct
    Joined: Apr 4, 2005
    Posts: 3,154

    bct
    Member

    ill bet there is not much left to learn after that.
     
  28. TBone69
    Joined: Aug 21, 2007
    Posts: 833

    TBone69
    Member
    from NJ

    Got the trans all buttoned up this weekend!


    [​IMG]

    Got some grade 8 hardware coming from McMaster to bolt trans to Cling’s adapter and adapter to motor.

    Trans going in this coming weekend.


    Sent from my iPhone using The H.A.M.B. mobile app
     
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