Register now to get rid of these ads!

Projects 1934 3 window HighBoy Build Begins

Discussion in 'The Hokey Ass Message Board' started by geoking, Dec 12, 2012.

  1. geoking
    Joined: Nov 12, 2008
    Posts: 717

    geoking
    Member

    Well, we didnt win! smile. We received a class "participant" award. I'm happy for the winner.....But have to admit that being runner up'ish is disappointing. It was a tough class and we had a great time. The coupe showed nicely and I was surprised to see people from my past that I hadn't seen in over 20 years. It was also very nice to make a new friend with a fellow that won his class with a 36 roadster.

    A huge thank you to Dustin, Fred and Josh. I enjoyed your company and appreciate your friendship.

    Warmest Regards,
    George



     
  2. daddio211
    Joined: Aug 26, 2008
    Posts: 6,012

    daddio211
    Member

    The car looked absolutely amazing, George. You all did a beautiful job on the build and have every right to be proud.

    My wife and I came by twice hoping to catch you but missed you both times. We'll catch you sometime soon.

    My '27 T Roadster build: www.jalopyjournal.com/forum/showthread.php?t= 734383
     
  3. s55mercury66
    Joined: Jul 6, 2009
    Posts: 4,343

    s55mercury66
    Member
    from SW Wyoming

    George, the car is beautiful, and you and everyone who helped make it that way did a great job. Sorry you didn't come home a winner, but it's been great following this thread. :D
     
  4. George, you don't need a trophy to tell yourself, Dustin, Fred and Josh that you're winners. The "award" is that beautiful 34 coupe that has been reborn to be enjoyed. I have really enjoyed following along on the build; thank you for sharing it with us.

    Blessings,
    David
     
  5. daddio211
    Joined: Aug 26, 2008
    Posts: 6,012

    daddio211
    Member

    Oh he came home a winner, he brought that car home! Trophies mean nothing.

    My '27 T Roadster build: www.jalopyjournal.com/forum/showthread.php?t= 734383
     
  6. dirty old man
    Joined: Feb 2, 2008
    Posts: 8,910

    dirty old man
    Member Emeritus

    X2 That's about the nicest most detail oriented hot rod I've ever seen. Wish I could have seen it live at the show!
     
  7. 1947vert
    Joined: Sep 20, 2007
    Posts: 250

    1947vert
    Member
    from Minnesota

    George, your car was amazing and I feel lucky to have seen the car in person after following the build here on the HAMB. Now comes the best part driving it! ENJOY
     
  8. ScooterCO
    Joined: Nov 28, 2007
    Posts: 89

    ScooterCO
    Member
    from Parker, CO

    Can't drive a trophy.. Go drive your car!
    An amazing build, thank you for sharing it with the rest of us.
     
  9. s55mercury66
    Joined: Jul 6, 2009
    Posts: 4,343

    s55mercury66
    Member
    from SW Wyoming

  10. Bulletnose26
    Joined: Jul 21, 2013
    Posts: 170

    Bulletnose26
    Member

    Thank you very much, for the time spent, sharing this build. Congratulations to your team of builders, they built one heck of a HotRod!
    I hope the story doesn't end here......get out and drive that thing!
     
  11. daddio211
    Joined: Aug 26, 2008
    Posts: 6,012

    daddio211
    Member

    We all knew that, there couldn't be anything bad said about George or his car. :cool:
     
  12. Dan Greenberg
    Joined: Aug 18, 2008
    Posts: 8,014

    Dan Greenberg
    Member
    from Parker, CO

    Here is how she looked displayed at the show.

    [​IMG]
     
  13. loudbang
    Joined: Jul 23, 2013
    Posts: 40,292

    loudbang
    Member

    A couple more photos from bangshift.

    1934 (800x533).jpg click to enlarge photos

    1934 a (800x533).jpg

    1934 b (800x533).jpg
     
  14. geoking
    Joined: Nov 12, 2008
    Posts: 717

    geoking
    Member

    Thank you all, for the very nice comments....it is very much appreciated.

    Everyone has now made it home safe and sound. We still have work to do to finish the coupe.

    1. She has only been driven in first and reverse. It will need to be road tested for adjusting the 700r4 automatic transmission throttle valve cable.

    2. She will need to go for a front end alignment.

    3. The heater hose fitting at the back of the head leaks. Not a hard fix , but a PITA to get to it via the fire wall.

    4. There is an oil leak that we do not know if it is the rear main seal or the oil pan from the last minute thrashing to get the timing fixed.

    5. The drivers side door latch needs adjusting to pull the door closer for sheet metal alignment .

    6. She needs to be put on a dyno and be performance tuned.

    7. Last ....but "NOT A HAVE TO".... the wiring harness for the EFI needs to be shortened.

    That's about it...smile

    Best Regards,
    George
     
  15. Great to see you at GNRS George!
    The car is amazing!

    ImageUploadedByH.A.M.B.1391018406.001027.jpg
     
  16. geoking
    Joined: Nov 12, 2008
    Posts: 717

    geoking
    Member

    Mike ,
    Thank you for stopping by. It was nice to see ya'll.

    For those that don't know who's whom in the photo...I'm the chubby guy on the left. Mike is on the right. The nice lady in the middle is Mike's sweet heart.(Amy)

    Regards,
    George


     
  17. fryguy
    Joined: Nov 26, 2005
    Posts: 1,235

    fryguy
    Member

    . Seems like the car went over well and it looks like you had a blast at GNRS. In my book, thats a big success
     
  18. geoking
    Joined: Nov 12, 2008
    Posts: 717

    geoking
    Member

    Thank you Fryguy,

    It was a nice effort and I am glad we did it. What's important for me now is to bring the build to completion.

    3 items on the punch list are now complete.

    1. The anti freeze leak has been repaired by replacing the gasket on the heater hose adapter plate at the rear of the head. PLUS adding sealant to the threads on the two bolts. Not sure which area was the actual culprit?
    Either way.....cross this off the to do list.

    2. The fuel gauge wasn't working and replacing the sending unit has cured this. Not sure why a new unit wasn't working. Maybe it was just a grounding issue. check this one off the list!

    3. The drivers door did not close flush and this was caused by the latch not pulling in tight enough with the new door seals. The latch was adjusted and all good now.

    We still have the following to address.

    1. Rear main seal leaks. We are hoping the seal will swell and fix itself before the dreaded effort to replace. ON hold for now. We shall see.
    2. Front end alignment will be scheduled
    3. putting her on a chassis dyno and tuning the fuel injection for peak performance will be scheduled
    4. EFI wiring harness will be replaced with a new one to eliminate the 42 inches that is coiled up under the dash. I KNOW IT WORKS!. But , it just isn't a clean install. Holley Sells a kit to build your own. I am dreading this but just cant leave it alone.
    5. I hate my Limeworks turn signals. Not sure if it is their product issue or our install? When you turn them off , it takes a moment for the power to bleed off and the flasher on the end of the arm to quit flashing. I want the thing to stop flashing IMMEDIATELY. smile. It's low on the priority list but still on the list just the same.
    6. The TV cable to the 700r4 still needs to be road tested and adjusted.

    That covers all the issues and when all are completed , then I will be satisfied. smile.

    Warm Regards to all that have been following the build. I really appreciate the kind words and support.
    George






     
  19. s55mercury66
    Joined: Jul 6, 2009
    Posts: 4,343

    s55mercury66
    Member
    from SW Wyoming

    It's been fun watching this come together. Thanks for sharing.
     
  20. geoking
    Joined: Nov 12, 2008
    Posts: 717

    geoking
    Member

    http://youtu.be/C8TVysVzUhE


    She's been in the after the show detail clean up stage and is almost fully de bugged. Today was tranny TV cable tune in / adjustment day.

    So much fun! 25 MILES ON THE ROAD TODAY!

    She still needs to have 3 items completed...chassis dyno and rear main oil leak and a new gasket water leak ( easy fix).

    ALMOST THERE GUYS!

    Loving the vroom part....

    George












     
    Last edited: Feb 18, 2014
  21. daddio211
    Joined: Aug 26, 2008
    Posts: 6,012

    daddio211
    Member

    <iframe width="640" height="480" src="//www.youtube.com/embed/C8TVysVzUhE" frameborder="0" allowfullscreen></iframe>

    Way cool!
     
  22. loudbang
    Joined: Jul 23, 2013
    Posts: 40,292

    loudbang
    Member

    Now it even sounds like a Hot Rod.
     
  23. amen!
     
  24. ScooterCO
    Joined: Nov 28, 2007
    Posts: 89

    ScooterCO
    Member
    from Parker, CO

    The sound is awsome! Great looking ride..
     
  25. geoking
    Joined: Nov 12, 2008
    Posts: 717

    geoking
    Member

    Crocodile Tears.... She isn't making the power that she should and a compression test shows bad news on one bank. Please find TODAYS pictures. There is a little good news in that the oil leak will be easy to fix. grin.
    regards,
    George





     

    Attached Files:

  26. JasonCarGuy
    Joined: Apr 16, 2008
    Posts: 131

    JasonCarGuy
    Member

    Looks like a damage piston?


    Posted using the Full Custom H.A.M.B. App!
     
  27. fryguy
    Joined: Nov 26, 2005
    Posts: 1,235

    fryguy
    Member

    Not sure if I'm pointing out the obvious but I think it needs heads on the engine in order for it to run properly?:D
     
  28. geoking
    Joined: Nov 12, 2008
    Posts: 717

    geoking
    Member

    Good Morning Jason,
    A close inspection shows that the piston is ok. #3 and #5 cylinders have extremely low compression and we are betting on ring issues as the heads are newly rebuilt and look great. It's off to the Greeley Engine shop for a little discovery effort. I hope that it isn't anything major. I learned a valuable lesson and will not trust a purchased short block assy. in the future. In hind sight, it would have been a sound investment to have pulled it down at receipt for a thorough going through. The good news is that we have time to get her fixed and back together for the upcoming season.

    While disappointed, It wasn't the Custom Auto guys fault. The blame falls squarely on my shoulders for my failure to insure it was right.

    We shall see. I will report back as we learn more.

    Regards,
    George

     
  29. geoking
    Joined: Nov 12, 2008
    Posts: 717

    geoking
    Member

    Here's the finding.
    LACK OF OIL DURING OUR INABILITY TO GET HER STARTED caused cylinder wash. When we had timing issues and pushed too much gas down her throat we screwed up. The fact that the intermediate shaft was too short and we swapped out early may have also contributed.

    There is no major damage and the block will be honed, new rings , new seals/ gaskets and re assembly.

    As a precaution, we will use a four barrel intake for running her in on the engine shop dyno before going back with the EFI.

    Ill need to buy a set of spacers for this as I am running 331 heads on the 392.

    A little relief to know what happened. smile

    regards,
    George



     
  30. s55mercury66
    Joined: Jul 6, 2009
    Posts: 4,343

    s55mercury66
    Member
    from SW Wyoming

    Glad to hear you have found no more than that, George. Also, I have been looking at your avatar for over a year now, and just recently found out is a Ford. I have been thinking it was a Plymouth business coupe all this time. Now I have to get new glasses.
     

Share This Page

Register now to get rid of these ads!

Archive

Copyright © 1995-2021 The Jalopy Journal: Steal our stuff, we'll kick your teeth in. Terms of Service. Privacy Policy.

Atomic Industry
Forum software by XenForo™ ©2010-2014 XenForo Ltd.